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ACLines 64 ready to download
Posted on 11th September 2017 11:56The latest edition of the AC Locomotive Group's magazine, ACLines, is now available for download by members.
Please log on to the forum and member's download area via http://www.aclocogroup.co.uk/forum/login.php?redirect=../member.php
86101 returns to service
Posted on 23rd June 2017 12:54
The ETS repairs to 86101 have been completed and the locomotive has been released from HNRC Barrow Hill.
86101 is currently en route to Willesden/Wembley to resume Caledonian Sleeper ECS duties alongside 87002.
Update on Class 89 Restoration
Posted on 22nd April 2017 07:34
AC Locomotive Group Volunteers are continuing the restoration of the Class 89. The testing and investigation phase of the restoration work is nearly complete, with all the locomotive’s systems having been inspected and tested.
Preparations are underway for the overhaul of the bogies with the removal of the Primary Suspension Dampers having recently been removed. The Secondary Suspension Dampers were removed when the locomotive was lifted in 2016.
Testing of the Rheostatic Brake Stacks has shown that both units have failed. Following removal from the locomotive, Brake Stack #2 was stripped down and inspected, the inspection has shown that there had been a catastrophic failure of the Fan Motor which in turn caused serious damage to several resistor elements. The Fan Motor on Brake Stack #1 has also been found to be badly damaged. We have reviewed the service history of the 89 and have found that there were persistent problems with the Fan Motors throughout the locomotive’s life, so the decision has been taken to rebuild the Brake Stacks with ‘new’ motor and fan assemblies of the type used in Classes 86 and 87. CAD work is in hand for the redesigned Brake Stacks and a mock-up will be produced to check the mechanical fit of the revised Brake Stack into the locomotive.
A number of obsolete components have been identified for replacement; the Voltage Transducers for each Traction Motor are in the process of being replaced – access to the Voltage Transducers can only be achieved by dismantling the Motor Contactor Cubicles so this is a time-consuming job. The ACLG Engineering Team has identified several areas where reliability improvements can be made by replacing and modernising components and sub-systems.
Repairs to various items of cab equipment have been completed; the brake controllers and the switch panels on both desks have been worked on, most of the equipment is in good condition. Some cosmetic work remains to be undertaken on repairing various interior trim panels before they can be reinstated.
Cleaning of various items of electrical equipment and equipment ventilation systems has been undertaken by ACLG volunteers. Small amounts of corrosions on the interior of the cab roof framing, under the cab floor and in the Brake Stack areas has been cleaned up and prepared for repainting.
Our thanks to our volunteers for their work over the last year and to our industry partners at Bowers Electrical, Bralesford Engineering Services, Fletcher Moorland and HNRC without whose help the work on the 89 would not be possible.
Picture: (Top Left) ACLG Volunteers removing Primary Dampers, (Bottom Left) Primary Dampers removed for refurbishment, (Centre, Top) Rheostatic Brake location, (Centre Bottom) CAD Model of new Rheostatic Brake Stack, (Right Top) Overhauled Brake Controller and (Bottom Right) One of our younger Volunteer’s Homework – preparing cab interior panelling.
Testing of Class 89 Armature Converters
Posted on 12th March 2017 09:54
The 11th March represented a milestone in the preservation history of 89001 with its’ Armature Converters being energised to test that they were operating correctly. Testing the Armature Converters without a 25kV supply and no traction motors to load the converters has required several months of preparation work. Arrangements were made to permit the injection of 240V AC into individual bridges on the Armature Converters, the bridge DC outputs were loaded by connecting them to the Load Bank (which is usually testing Diesel Electric Locomotives) at HNRC Barrow Hill. Control of the Armature Converters was via the 89’s microcontroller, with a hand-held control device being used instead of the locomotive’s master controller.
The testing proved successful with the Microcontroller and of the devices in both Armature Converters operating correctly.
Our thanks to Bralesford Engineering Services and HNRC for their assistance with this work.
Picture (clockwise from left); ACLG Volunteers installing power connection on to Armature Converter #2, Installation above Armature Converter #1, Hand-held control device connected to Microcontroller, Microprocessor Thyristor Firing Card sending signal Armature Converter #1 and DC current being recorded flowing to the Load Bank resistors.
Brush Traction provide technical support to Class 89 restoration
Posted on 20th October 2016 09:04
After several months of negotiations, we have completed an agreement to obtain technical assistance from Brush Traction to help with our overhaul of 89001.
We are in the very rare position of being granted access the Brush Traction design archives. We have been loaned the design file for the locomotive and a considerable amount of supporting correspondance relating to its' service with both BR and GNER.
We gratefully acknowledge the considerable contribution that Brush Traction and Wabtec have made to the Class 89 restoration project.
87002 to work Paralympic Special
Posted on 17th October 2016 07:41
As part of the Olympic and Paralympic celebrations 87002 will operate a special service, being provided by Caledonian Sleeper, from Manchester Piccadilly to London Euston on 18 October. The service is scheduled to leave Manchester at 07:10, further information on timings can be obtained from Real Time Trains.
ACLG Youtube Channel
Posted on 11th September 2016 10:51
We have launched our own Youtube Channel to give deeper coverage of our restoration of some of the locomotives. In the first video, the 89 starts to wake up at Barrow Hill https://www.youtube.com/watch?v=jVwkkm2r_88
Class 89 Lifted
Posted on 2nd August 2016 08:15
There has been further progress on the Class 89 today with the locomotive being moved into the HNRC workshops at Barrow Hill to allow the locomotive body to be lifted from its’ bogies and the removal of traction motors #4-6. The traction motors will be sent to Bowers Electrical for an overhaul.
The components removed from 89001; the Field Converters and Rheostatic Brake Stacks are already with Fletcher Moorland and Bowers Electrical for assessment. Assessment of the Rheostatic Brake Stacks has focussed on the brake stack from #2 end, this stack has been found to have sustained serious damage in service which will necessitate a rebuild of both the resistor and fan motor sections of the stack. Bralesford Engineering Services and ACLG Electrical Engineers are investigating a number of design improvements to be incorporated into both of the Rheo Brake Stacks to remove the failure modes that lead to #2 brake stack being damaged.
An extensive survey of the locomotive’s running gear is underway, with both axles and bearings being subject to an thorough inspection. With the locomotive in a partially dismantled condition the opportunity will be taken to assess the condition of the various power smoothing and surge suppression circuits to ensure that their capacitors are in good condition; a number of the circuits are only accessible by removing the roof or lifting their equipment frames from the locomotive.
Above Left: #2 End Rheo Brake Stack being removed (Courtesy Bralesford Engineering Services)
Above Right: 89001 body lifted from the bogies inside HNRC workshop (Courtesy Bralesford Engineering Services)
Update on Class 89 Restoration
Posted on 25th July 2016 10:51
The overhaul of 89001 took a major step forward today with the locomotive moving on to the lifting pad outside the HNRC workshops at Barrow Hill to have its’ Field Convertors and Rheostatic Brake Stacks removed. The complete Field Convertor cubicles will be moved to Fletcher Moorland for a specialist electronics overhaul and testing to ensure that will ensure that each convertor is performing correctly before being returned to the locomotive. The Rheo Brake Stacks will be moved to Bowers Electrical for overhaul and repair; recent assessment work undertaken by ACLG volunteers has highlighted that there is likely to be damage to the #2 end brake stack – the resistances of a number of stages are outside of expected values.
A considerable amount of other work has also been undertaken by staff from Bralesford Engineering Services, HNRC and volunteers from the ACLG. Testing and inspection of the air brake systems has shown that it is operating correctly and the system is close to tolerance on air leakage. Specialist equipment is being developed to test the electronic ‘brake blending’ control that ensure correct operation of the friction and rheostatic braking systems.
The locomotive has been attached to various shore supplies to allow various 240V equipment to be tested; both battery chargers work and a number of the cooling fans have been test run. Last weekend, following the tracing and rectification of a short circuit on #2 end air conditioning unit it has been possible to test the air conditioning units for both cabs, achieving a cab temperature of 21C when the external temperature was 28C with air conditioning units that have stood idle for 16 years was a pleasant surprise.
The Microprocessor Control and its’ associated electronics has been surveyed, with considerable time being taken to assess the condition of individual cards and to investigate/understand the operation of the cards and the entire control system. A defect that was preventing the Microprocessor from ‘booting up’ has been repaired by the ACLG’s electronics specialist and the Microprocessor is now operating normally. The 1980s vintage Oyster terminal that is used to interrogate the Microprocessor has been replaced with modern software that is run on a laptop. Considerable efforts are being made to develop an ‘electronics strategy’ for the 89 to ensure good reliability and component resilience.
In addition to the major works and investigations there are various more general works underway including cleaning various filters, removing obsolete equipment, etc with a mixture of contractor and volunteer labour being used.
The unique and significantly ‘prototype’ nature of the 89 means in addition to the usual collection of spurious faults inherent in any locomotive under restoration there can be a number of puzzling and unusual problems, more learning for all involved – even for ex Brush staff. Whilst we have developed an extensive list of ‘areas of concern’ relating to the 89 we are pleased that in many areas the locomotive appears to work as intended.
Above Left: #1 End Rheo Brake Stack being removed (Courtesy Bralesford Engineering Services)
Above Right: #2 End Field Convertor being removed (Courtesy Bralesford Engineering Services)
89001 Microprocessor Control Investigations
Posted on 11th June 2016 06:09
Work on recommisioning 89001 continues with a number of exam and inspections having been completed. One area of the 89 that has been identified as a risk to the locomotive's overhaul is the Microprocessor control system. Whilst the Microprocessor has been powered up and partially tested in the past it represents a significant 'unknown quantitity' in respect to its' current condition and function. In recent weeks the 89 has been powered up several times and on each of these the Microprocessor has failed to sucessfully 'boot up' and indicated an error somewhere in the locomotive's traction control system.
Following an inspection of the various cards that comprise the Microprocessor Control Rack (in addition to a card containing the Motorola 68000 microprocessor there are a number of buffer and input/output translator cards) it was concluded that the fault could not be resolved on the locomotive and the decision was taken to remove the entire Microprocessor Rack for assessment and fault finding off site; the picture shows the Microprocessor Control Rack removed from the locomotive prior to dispatch to the ACLG's electronics specialist.
89001 Control Circuits Energised
Posted on 15th May 2016 02:59
Following recent work by volunteers and staff from both Bralesford Engineering Services and HNRC we have successfully re-commissioned the Control and Field Convertor Batteries on 89001. Having the batteries in an operational condition is an important step in that it enables the locomotives' battery chargers and a number of other control systems on the locomotive to be energised and tested.The picture shows the control desk at #1 end energised on 14th May while the locomotive microprocessor controls were undergoing testing. Work on the bogies and brake systems on the 89 is also progressing.
As items are serviced and inspected the considerable number of documents relating to the design and maintenance of the locomotive in the ACLG’s possession are being reviewed to ensure that they reflect the condition the locomotive is now in and to establish a thorough understanding of the locomotive for maintenance and fault finding.
Class 89 Restoration
Posted on 28th April 2016 10:50
The AC Locomotive Group (ACLG) is pleased to announce progress on the restoration of locomotive 89001 and the imminent commencement of major repair work.
Over the last few months ACLG volunteers have completed an assessment of the condition the locomotive, reconditioned the battery systems, removed the obsolete NRN radio system from the cabs and commenced refurbishment of the cab interiors.
The locomotive will shortly be moved to the workshops of Harry Needle Railroad Company (HNRC) for the first stage in heavy overhaul works to be undertaken. The overhaul work will concentrate on two key areas; bogies and traction power equipment. Bogie work will comprise of an ultrasonic inspection of the locomotive axles and the locomotive being lifted to allow the removal of traction motors 4-6 for overhaul (traction motors 1-3 have already been removed and overhauled). The traction power equipment overhaul work will require the removal of the locomotive roof after which the field convertor cubicles, rheostatic brake stacks additionally the cab air conditioning units will both be removed. Removal of the field convertor cubicles will enable the repair of field convertors 1, 3, 4 and 6 to be completed; ACLG volunteers having already removed field convertors 2 & 5 by hand and both of these units have already been overhauled. Overhaul of the traction motors will be undertaken by Bowers Electrical and the overhaul of the field convertors will be undertaken by Fletcher Moorland.
In addition to the volunteer technical and project management team from within the ACLG Tim Bralesford (Bralesford Engineering Services) will be providing project management and technical services. Tim has unrivalled knowledge of the 89 as he worked on its design, construction and commissioning in the 1980s and its overhaul and re-commissioning in the 1990s.
The restoration of the Class 89 is a major project with considerable complexity and as such a date cannot be set when the locomotive will be returned to operational condition.
A technical ‘walk through’ of the locomotive (including some of the equipment to be repaired) is on Youtube at https://www.youtube.com/watch?v=hxbv_-QCa6A
Funding for the repairs to 89001 is being provided from funds generated by the mainline operations of locomotives 86101, 86401 and 87002, the sale of locomotive 86213 and from donations to the AC Locomotive Group.
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